Boost Leak
Intercooler is the new design. I managed to narrow it down to the boost bolt (lack of thread tape) and the intake horn gaskets. Buttholes didn't replace them when they did my injectors. 

Damn leak tester leaked so much, it was hard to get an accurate test. I did replace the intake horn gaskets, and wrapped the bolts with some thread tape. It's still hitting 1200 too easy. I just reset the APPS, and I'm going to take some fine sandpaper after the EGT probe. If that doesn't do it, that leaves it down to some lying azz gauges.
APPS reset, cleaning the EGT probe, cleaning the wires down by the AC compressor. Neither did nothing.
So that leaves these possibilities:
lying gauges
faulty fca
faulty apps
timing
So that leaves these possibilities:
lying gauges
faulty fca
faulty apps
timing



