Ford Powerstroke 03-07 6.0L Discussion of 6.0 Liter Ford Powerstroke Turbo Diesels

Need help with sluggish and a slight miss.

Thread Tools
 
Search this Thread
 
  #1  
Old 04-12-2013, 09:23 PM
EricC's Avatar
Diesel Enthusiast
Thread Starter
Join Date: May 2011
Location: Pc florida
Posts: 131
Likes: 0
Received 1 Like on 1 Post
Default Need help with sluggish and a slight miss.

I have a 2004 f250 6.0 has EGR delete and oil cooler replaced maybe 6,000miles ago. I have always thought that my truck was louder than most other 6.0 as far as engine noise. lately i have noticed a slight miss at idle, as well as the engine has dies a couple times when i would let off the gas to turn or what not, but has always started right back up like nothing had happen. The truck is also very sluggish once it goes into overdrive, and seems like it is a little down on power i do have a sct with custom tunes from innovative, but i have returned it to stock since i have noticed the problems, i am also running rotella t5 10w30. thanks for any help .
 
  #2  
Old 04-14-2013, 12:05 AM
POWER-STRUCK's Avatar
Diesel Enthusiast
Join Date: Mar 2013
Location: Indiana
Posts: 161
Likes: 0
Received 4 Likes on 4 Posts
Default

did you check ficm voltage?
 
  #3  
Old 04-14-2013, 07:24 AM
Adrenaline junkie's Avatar
Diesel Wrench
Join Date: Nov 2012
Location: South New Jersey
Posts: 536
Received 19 Likes on 19 Posts
Default

Check fuel pressure at bowl too. I had misfire, hooked up snap on scan tool and had two injectors misfiring. Kept searching, Turns out my airdog pump went bad! . . New warranty one going in today!
 
  #4  
Old 04-14-2013, 04:00 PM
EricC's Avatar
Diesel Enthusiast
Thread Starter
Join Date: May 2011
Location: Pc florida
Posts: 131
Likes: 0
Received 1 Like on 1 Post
Default

Yes i did text the FICM and its good. I replaced it maybe ayear ago with one from Mike, I have not checked the fuel pressure yet. I did put it on the Snap-on soulus pro, and did not find any misfires and passed all test, i did buzz test but i have read that the best time to run that test is on first start up on cold motor. Going from the 15w40 to the T5 10W30 should not have any affect on it should it? how bout the icp sensor? when i had it on the scanner the icp desired and the actual all looked good, i did not run it down the road while hooked up to see what happens.
 
  #5  
Old 04-14-2013, 08:22 PM
Adrenaline junkie's Avatar
Diesel Wrench
Join Date: Nov 2012
Location: South New Jersey
Posts: 536
Received 19 Likes on 19 Posts
Default

Did you check memory codes? That's where I found misfire codes on 6,7,8 cyl . . Due to lack of fuel . . Got new airdog installed today. . Fuel mileage back up to 15.4 from 13.8 with stocker on lie o meter and much smoother. . . Please keep us informed of your particular outcome!
 
  #6  
Old 04-14-2013, 08:39 PM
EricC's Avatar
Diesel Enthusiast
Thread Starter
Join Date: May 2011
Location: Pc florida
Posts: 131
Likes: 0
Received 1 Like on 1 Post
Default

Yes i did check for memory codes, all it had was one for the FICM because its not the original one in it. Was the air filter causing yours not to get enough fuel? I ordered some Archoil AR9100 tonight going to see if maybe its an injector
 
  #7  
Old 04-14-2013, 08:52 PM
Adrenaline junkie's Avatar
Diesel Wrench
Join Date: Nov 2012
Location: South New Jersey
Posts: 536
Received 19 Likes on 19 Posts
Default

airdog was seized. died while idling with modis connected doing diagnostics. popped Fuel filter on engine and was empty. i hooked stock pump back up since i bypassed it before it totally died and got mobile till ad replacement. I use hot shot secret and rev x with Rotella 5-40 synthetic oil . . For years . . Almost 200,000 miles on stock original injectors. And power service in fuel, with antigel in colder months. Felt really good on hour and half ride home! I hear arch oil is good too . . Anything to help keep clean oil and prevent stiction is a good thing in a 6.0. . . . .
 
  #8  
Old 04-14-2013, 09:02 PM
EricC's Avatar
Diesel Enthusiast
Thread Starter
Join Date: May 2011
Location: Pc florida
Posts: 131
Likes: 0
Received 1 Like on 1 Post
Default

Mine has 120k on it and knock on wood this is the only problem i have had, i will try that and see how it does also gonna change the fuel filter too even know it is not due yet. The air filter is old but the change indicator has not went off wondering if it needs changing anyways .
 
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
Brian54
Diesel In Distress - Support Ticket
2
06-27-2015 06:21 PM
Bighouse
Ford Powerstroke 03-07 6.0L
1
04-09-2015 06:51 PM
OBSBEN
Ford Powerstroke 94-98 7.3L
0
12-31-2014 11:35 AM



Quick Reply: Need help with sluggish and a slight miss.



All times are GMT -5. The time now is 04:27 AM.