12 Valve 2nd Gen Dodge Cummins 94-98 Discussion of 12 Valve 5.9 Liter Dodge Cummins Diesels with P7100 Injection Pumps

bad stumple in Park?

Thread Tools
 
Search this Thread
 
  #21  
Old 01-20-2012, 12:19 PM
turbo2332's Avatar
Diesel Bomber
Thread Starter
Join Date: Jun 2011
Location: Indiana
Posts: 2,171
Received 104 Likes on 101 Posts
Default

think i may have figured some of this out. timing was stock at 12.3 on my truck. just put it to 16. when the sun comes back out we shall see what it did. maybe MPG will go up about 10 LOL
 

Last edited by turbo2332; 01-20-2012 at 12:56 PM.
  #22  
Old 01-20-2012, 12:46 PM
tower_ofpower's Avatar
Diesel Bomber
Join Date: Jul 2009
Location: Kingwood, WV
Posts: 1,861
Received 86 Likes on 80 Posts
Default

16.5 maybe 17 would have been my preference, but then again I love me some timing . I thought stock was higher than 13ish? And unfortunately if that's "stock" then why don't more factory spec trucks have this issue? Idk if it will actually take care of your problem, it may dramatically reduce the issue tho. A step in the right direction


Sent from my iPhone using Tapatalk
 
  #23  
Old 01-20-2012, 12:59 PM
turbo2332's Avatar
Diesel Bomber
Thread Starter
Join Date: Jun 2011
Location: Indiana
Posts: 2,171
Received 104 Likes on 101 Posts
Default

i thought it would be higher too? i set it as if it were 13.5 like i figured it would be and after all was said and done i read the tag and low and behold 12.3. so it comes out, if im reading my paper right in the high 15's. it will get turned up a bunch more when the head work gets done. oh and i ordered some DV's to throw in there to. we shall see if that was a culprite aswell
 
  #24  
Old 01-20-2012, 03:53 PM
tower_ofpower's Avatar
Diesel Bomber
Join Date: Jul 2009
Location: Kingwood, WV
Posts: 1,861
Received 86 Likes on 80 Posts
Default

You did order or do have the socket for the DV holder right?


Sent from my iPhone using Tapatalk
 
  #25  
Old 01-21-2012, 09:24 PM
turbo2332's Avatar
Diesel Bomber
Thread Starter
Join Date: Jun 2011
Location: Indiana
Posts: 2,171
Received 104 Likes on 101 Posts
Default

the stumble was a bad OFV. thanks for the insite fellas
 
  #26  
Old 01-22-2012, 01:42 AM
tower_ofpower's Avatar
Diesel Bomber
Join Date: Jul 2009
Location: Kingwood, WV
Posts: 1,861
Received 86 Likes on 80 Posts
Default

Good to hear, didn't even think of suggesting your OFV bc you said plenty of power and smoke. Low fuel pressure I figured would have caused power loss across the band.


Sent from my iPhone using Tapatalk
 
  #27  
Old 01-22-2012, 08:35 AM
turbo2332's Avatar
Diesel Bomber
Thread Starter
Join Date: Jun 2011
Location: Indiana
Posts: 2,171
Received 104 Likes on 101 Posts
Default

the lift pump must have been able to over come the leaky valve unce up in the rpms is all i can figure
 
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
|WYG|SS
24 Valve 2nd Gen Dodge Cummins 98.5-02
5
07-04-2015 08:31 AM
Diesel Bombers
Latest Automotive Industry News
0
03-18-2015 02:00 PM
Diesel Bombers
General Diesel Related
0
02-05-2015 12:10 AM
cdpowers
5.9 Liter CR Dodge Cummins 03-07
6
01-23-2015 01:42 PM
12vbomber
12 Valve 2nd Gen Dodge Cummins 94-98
3
11-11-2014 10:58 AM



Quick Reply: bad stumple in Park?



All times are GMT -5. The time now is 02:13 AM.