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kars3434 04-24-2013 10:12 AM

01 ram no power
 
01 ram 2500. I replaced the tappet cover gasket. To do this I had to remove the injector pump (unplugged) and the ecm (left plugged in). Put it back together, Was SURE of the key placement in the pump gear. I bled the filter to the injector pump (key on, hit start). I started the truck. It ran bad for awhile, I bled the injector lines at the head and it cleaned up. It starts and sounds great at idle but is like having a vw bug motor under the hood when I try it on the road. What the heck did I do? I've looked at all the plugins and am sure I got them all. I relearned the accelerator position sensor. I have not re-checked the key way. I guess that's my next step- but I'm sure it is right. I didn't move the crank nor the pump while everything was apart. Please help!
It doesn't leak oil any more but it sure ran good before I took it down. Gary (and Thanks!)

P.S. How can I follow any answers on this site? I know less about forums than Diesels.

MillerBoyzDiesel 04-24-2013 10:33 AM

Did you remove the intake elbow? Are you boost hose clamps tight?

kars3434 04-24-2013 11:51 AM

yes, the elbow came off. The clamps are for sure tight. Thanks for helping. I'm sure at a lose. I just bought this truck and like it a lot. Wish I hadn't broke it.
There are no codes.
One thing is I have an OBD scandisk reader plugged in and it wouldn't work at first fire up. The fuse to the cig lighter had blown. Don't know how I did this with the batteries (-) disconnected.

MillerBoyzDiesel 04-24-2013 11:59 AM

usually the cig fuse pops because of people pluggin in phone chargers and other accessories in that port. Are the intake heater gaskets at the elbow damaged or not sealing?

kars3434 04-24-2013 03:37 PM

I didn't replace the heater gaskets. They were clean and looked real good. I don't think I have an intake leak but I'll ck again.

The obd scandisk worked fine before I did this job but not after. The power that this gauge uses in the obd plug-in comes from this cig fuse. At least as soon as I replaced the fuse, the scandisk lite up.
Thanks again.

RanchhandTCR 04-24-2013 07:46 PM

you didint break any wires to the pump or anything like that did you?

kars3434 04-25-2013 09:59 AM

The bottom mount bolt of the ecm was digging in the wiring harness just 4 inches below the plug that goes into the ecm. I bent the strap bracket that holds that harness for a little clearance. This truck has 250K miles and maybe the wires were too brittle to rearrange like that. I'll have to run the wires from ecm to pump???
I drove the truck today with the idea MillerBoyz gave me about loss of boost and that is what it seems like it runs like - just no power. I'll put a pressure gauge on it also. Thanks for your help.

RanchhandTCR 04-25-2013 07:26 PM

All it takes is one wire to fray, but do what miller boy said also.
Keep it Simple.

kars3434 04-26-2013 09:55 AM

I'll ck all these things out but I'm busy until the week end. Thanks for your help. I'll fix it and I'll report the fix (my screw up!).

kars3434 04-27-2013 10:08 AM

??'s. I cked the lift pump at the schrader valve on the injector pump and found 10#. not running. I had almost that at idle and at full throttle I went down to 2 lbs. I read that this is low and know I'll have to address this but my truck ran fine before I pulled the injector pump and it must have had the same pressures from the lp. Is it possible that this low pressure could be the problem?

Also, is it possible that the pump gear turned a tooth while I was jiggling the injector pump back in it?

Thanks again.

MillerBoyzDiesel 04-29-2013 08:39 AM

deff. need to get that lp replaced before you kill your new injection pump. I doubt the the gear jumped a tooth, that would be hard to do.

kars3434 05-03-2013 07:31 PM

Finally got back at this problem, I put a new LP (airtex) in the stock position. This has the LP in the tank with a full tank of fuel so I didn't want tp drop the tank or lift the bed So I just wired a relay into an airtex pump mounting it in place behind the filter. Now I have two LP's!! (both running). My pressure goes a little past 20 not running and stays right at 20 when running. Still don't have any power but I started here because I knew I needed more supply pressure to the Injector pump. If I get time this weekend, I'm going to check the pump key. It acts like it is in limp-in mode. Does it have one?
Thanks for your help.

kars3434 05-07-2013 02:40 PM

Final FIX! Of course you don't know how I love shoving rags down every hole when I tear things down. (but I do) Well, I counted the two rags out I put in the manifold under the heater but I still don't remember putting a rag down the intake tube towards the heat exchanger (but I did put one in there or it fell in or whatever). I guess I don't need to finish this post!
Thanks for your effort in helping me with this. I was going back down with it and pulled the elbo off and there it was in the housing sitting on top of the heater - a green rag with burn marks on it. Lucky for stupid me it didn't cause any problems.
\Gary

RanchhandTCR 05-08-2013 09:53 PM

The stuff that makes me laugh my ass off then want to strangle them lol.. No all is good Im glad it did not get past the heater or start a fire lol! Tip for next time dont stuff rags either tape them or use the clamps of the rubber boost hoses to cover the intake so you dont loose your rag! glad shes going..


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