no start and stumped! 07 5.9
#1
no start and stumped! 07 5.9
Ok, my truck won’t start, I’m stuck and I’ve stumped just about all my friends so I’m looking for some help here. I recently did pretty much all of the upgrades in my signature and 2 weeks after I pulled a number one miss-fire code so I changed my injector because it shot bad now it will not start at all. I checked and rechecked the tube I am confident it is fully seated. During my trouble shooting I broke the post off of the number 6 and I replaced that injector as well, also taking care to insure it was properly installed. I have cranked on it for a long time now so I am confident there is no air left in the system. I have installed a race plug in the rail to insure the check valve was not stuck open and bleeding off the pressure. I have shot all of the injectors individually, the wires individually, and the full circuits and everything is reading .5. I swapped the FCA, and removed the tuner still no start. The AirDog is running and sounds good. I have checked the stock filter bowl drain even though I have bypassed it with the AirDog and there was a little fluid draining but not much. I have no codes at all, not on the tuner or with the three key turns. I am very frustrated and kind of in a time crunch, any ideas will be welcomed! Thanks in advance!
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#6
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#9
they are clean I cleaned the battery terminals, V.C. gasket harness, map, its, ckp, and csp sensors with electrical connector cleaner both today and 3 weeks ago when i was installing the new parts.
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well I'm pretty sure I found the problem today. I started pulling the injectors today because I was going to take them all to be pop tested and one was dripping with fuel. my first thought was the tube wasn't seated but I had reseated it several times during this process and that didn't sit right with me. I decided to pull the nozzle off and take a look before trying to seat the tube again. When I did i realized this was the injector that had an alignment pin hole that was wallowed out and the pin had allowed the nozzle to turn enough that the pressure was no longer going through the hole. Well now I have, what looks like, a small crack on the nozzle and I need the rest of the injector too. I hope it will run when I am able to get the new one... thanks for all the suggestions!
---AutoMerged DoublePost---
well I'm pretty sure I found the problem today. I started pulling the injectors today because I was going to take them all to be pop tested and one was dripping with fuel. my first thought was the tube wasn't seated but I had reseated it several times during this process and that didn't sit right with me. I decided to pull the nozzle off and take a look before trying to seat the tube again. When I did i realized this was the injector that had an alignment pin hole that was wallowed out and the pin had allowed the nozzle to turn enough that the pressure was no longer going through the hole. Well now I have, what looks like, a small crack on the nozzle and I need the rest of the injector too. I hope it will run when I am able to get the new one... thanks for all the suggestions!
Last edited by crazyrocks; 03-17-2011 at 09:20 PM. Reason: Automerged Doublepost