2001 cummins low power!!!
I am currently working on a 2001 cummins for a friend and he has been trying to set it up as a pull truck. He has a few things done to it and they are as follows...
200HP injectors (not sure of brand) inter cooler and banks high ram intake with AFE air box no filter just a screen. High tech turbo 64/71/13 is what we were told is on there Quadzilla Adrenaline Smarty SO3 some kind of aftermarket VP44 FASS fuel sysytem EGT, fuel pressure, and boost gauge The problems we are having is high EGT's like 1200-1250 at cruising at 55mph LOTS or should I say TONS of pure black smoke What sounds like a timing issue. the exhaust kinda cracks when on it. and not a lot of power it is really a dog even at 50 pounds of boost. EGTS will run up to and above if allowed to 1600 degrees Fahrenheit We have removed the quad box not change and noticed insice the resitor looked fried. Also any of the setting did not seem to change anything so that is not hooked up right now. The smarty was turned up to 9 but tried that at stock and level 8 thinking it was getting too much timing no noticeable difference. That is all I can think of now does anyone have any ideas? P.S. It is slow as you know what |
i would get rid of the smarty for starters ........any codes
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no codes and we did remove the smarty and no difference or maybe about 100 degrees less EGTS
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a ton of smoke...........are you sure the charge air is making it to combustion????
noisy motor there, cant go by what you hear I would do a system pressure check..............amazing what you hear when the motor is off |
well did a system check and no leaks holds pressure well.
Still scratching head on this thing??? Also we set the smarty to the lowest level which is 1/2 power and we lost boost but not mush black and some EGTS like 100 degrees |
I would rid both boxes and see how she does.
another thought would be to check the MAP sensor...................if its wacked out then that could do this |
Well we are still trying to figure it out we took off the intake and looked for any blockages and none found we are really scratching our heads on this.
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Where are you measuring boost? It really sounds like you have an obstruction somewhere. The only time I had a similar issue was when I lost an intercooler boot. Different issue I know, but exact same results: high EGT's, tons of smoke and no guts. Good luck.
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We are checking on the intake elbow and plugged back in the quad box and the map sensor is reading the same as the gauge.
Checked the intake elbow, and nothing... That was wishful thinking, at least I was able to put the right length studs in the right places unlike the original installer... Been messing with Smarty tunes more. SW1(fuel saver) which yielded good results, which I believe is timing only.. EGTs were more tolerable at cruise (700-800 degrees), the truck is the quickest it has been yet, and it even Idles smoother... I almost forgot, less smoke too! So now I wonder if the VP is a tooth retarded? Would that explain everything? |
Updates??
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Please update.
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Im really wondering what happened
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Not sure yet what is going on with it we believe that the it could be due to the vp44 upgrade with out the upgraded injector lines.
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How much boost it making crusing? WOT?
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sounds like timing is off to me by the cracking you here in the exhuast i would have that pump checked
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Try running the Adrenaline Only.... :pca1:
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At WOT we are seeing 50lbs of boost and while cruising maybe 3-8lbs of boost.
As for the pump we have decided that we will have to look at it closer and we are thinking to try puting the stocker back on for sh*ts and grins We did try using the adrenaline only and we have concluded that the box is fried it does nothing. just a very expensive boost gauge |
Updates??
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Still trying to figure it out but i guess it could be closed for now. It will be a couple of weeks before we are able to get to the project of terring it apart.
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Going to close the thread for now. Thread publisher can reopen and update.
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Found the problems
Well after much time on the phone with too many companies a conclusion has been found.
The quad box is fried and that is to get fixed. $25 if the resistor only $100 if the whole board. Not bad The VP44 is the dragon flow and because the injector lines are not upgraded the fuel is not reaching the injectors at the correct time, duration and pressure. So those need to be upgraded. For the time being the stock VP44 is going back on to get us going for the time being untill the lines are purchased. Not to mention is is winter here so no truck pulls for a few months. I want to thank everyone for thier help and inform everyone of what the actual problem was |
Did returning it to stock help then??
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Returning it to stock helped slightly but still ran like junk. We will be taking it out here soon again with the stock pump reinstalled and going to see what happens.
Will keep you guys updated. |
:tu:
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Well initial conclution is that the stock pump is alrady running better...
Now just waiting for the roads to dry a little and will be taking it out to test. It is better though already!!! |
my 01 cracks like what you are talking about i am running 3000 tune but everything checks out nothing is wrong with mine infact in runs solid with the 3000 tune when i switched to this tune i started hearing the craking sound i can switch back and not hear it so i would think its normal for the pump stretch
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Still running ok??
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Yes it is running ok for now. This thread can be closed out I just wanted to finish filling it in with all the updates to cpmplete it....Hopefullly someone will search if they have a problem and this will help them.
Thanks Guys for alll the help. |
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