48re Gov Pressure
Drained my trans pan and added 5 quarts. Truck was shifting awful so I check dip stick and was low-added more new fluid and my truck is still shifting poorly now at full with fresh 8.5 quarts. I have a worse 1-2-1 shift and when going down the road TC wouldn't lock once (about 55mph)It did the first 2time lock fine but not the third time. I have read gov. Pressure solenoid could be the culprit but would that cause TC not to lock? My trans was shifting well before fluid swap so I am regretting my decision. Will borg Warner solenoid and new transducer potentially fix me or is there more going on? No CEL and trans has about 60k on rebuild.
|
how did the fluid look? smell bad? Normally fluid wouldn't change anything, Only time I have heard of it causing a problem was when the fluid was changed after the trans had worn clutches and slipping it only gets worse after a fluid change.
I would not think that's the case here, Did you have the filter out? |
Fluid looked decent- no burnt smell- I replaced filter about 5-7k ago and put up B&D pan- just dropped drain plug to drain. Magnet had little to no metal on it
|
really strange maybe it will get better after a little test driving. wish I could help more.
|
Replaced selonid and transducer and shifts great 1-3 but still no 4th- cts2 is reading 4th and locked at 55-60 mph but still 3rd gear 2700ish rpm
|
Replaced OD/TCC today- lock up works in OD but not shifting to 4th still :argh::argh::argh:
|
All times are GMT -5. The time now is 06:28 PM. |
© 2024 MH Sub I, LLC dba Internet Brands